The left thread on the rear axle, which looks undamaged, was 30 thousands of an inch (0.03″) too high! This could have been caused by heat stress or compression force when we pulled the rear hubs. The castle nut just refused to go on. Bruce suggested running a die along…
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Kriss Motors says:See https://krissmotors.com/Mk2/?p=7111 We used rivets to fasten the new strips instead...
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